The X Axis Construction


If you remember back to the beginning, I salvaged the stainless steel rod and printhead carriage from my Stylus Color.  These were to form the basis of my X axis.  The printhead carriage was plastic and needed a bit of trimming.  My plan was to mount a wooden platform on the printhead carriage that the Z axis could be bolted onto.  The mechanism would be a threaded rod with captive nuts as before.  I designed the printhead platform to obviously have mounting holes that matched up with the base of the Z axis bracket.  There would need to be a cutout to allow room for the threaded rod and lock-nut to protrude.

Here's the platform design:

X platform
Here's the side bracket design:
X side plate

Once again I made both side brackets at the same time by bolting them together.
Here are the finished pieces:
X plates

The platform is bolted to the side of the plastic carriage with aluminium plates and the Z axis was bolted to the platform while this was done to ensure alignment.
Here's the carriage before and after mounting:
X carriageX carriage mounted

Now the Z axis is unbolted, the bearings are fitted to the side plates, the Stylus Color stainless steel bar inserted and we see how it fits together:
X fit test

Next I make mounting brackets to hold the captive nuts - two as before to avoid backlash.  They're a nasty lash-up and I'm not proud of them.  I may well return to them one day and replace them with something better and more importantly, stiffer.
Here they are:
X captive leftX captive right

Now I reattach the Z axis and tweak everything to get it level:
X fit test2

Time now to work out how high above the Y axis to mount this.  To do that I need to bolt my miniature drill to the Z axis frontplate aluminium straps.  I also screw the side plates to a batten so that they stay upright.  It turns out that another piece of batten under either side raises the X axis by about the right amount.

Here's the result:
X height test

Here's a close-up of the drill mounting straps:
drill straps

Now I screw the bottom battens down and then screw the top battens to the bottom battens being very careful that the X axis remains perpendicular to the Y axis.  In retrospect, I probably shouldn't have mounted the blocks so far apart.  Despite the thickness of the 8 mm stainless steel threaded rod, it is still surprisingly flexible.  I wanted to maximise the drilling area though.  It's not like it sags though.  A better design would probably have a second smooth 1 cm stainless steel rod, like the Stylus Color one, attached to the front of the carriage.  The threaded rod would then only be used for moving the carriage and not supporting it as well.
So I replace the regular nuts with lock-nuts and trim the threaded bar to the right length.  Now comes my next mistake.  I can turn the X axis threaded bar with my fingers but how much torque is that?  I need to know because I haven't got a motor for this axis yet.  I don't have any performance graphs for my existing motors so they can't help me much.  I pored over datasheets, compared pull-in torques, holding torques, coil resistances, current per phase and make a stab at it.  Below is the result:

X wrong motor

It's not a complete disaster.  This Astrosyn Size 14 Mini Hybrid Stepper Motor (MY5602) is very powerful for its size.  It pulls 0.76 Amps per phase at 5 Volts too.  All that current in such a small volume makes it hot - very hot.  Fortunately it is rated as having a maximum temperature rise of 80 degrees centigrade.  Does it do the job though?  Almost.  Despite its size, it can move the X axis with the Z axis bolted on top most of the time.  Unfortunately, most isn't going to cut it.  If the motor misses steps, the holes will get drilled in the wrong places.  At least it was a cheap motor.  What it did do though was provide me with a reference level of the required torque.  I did err on the side of caution and the motor I bought to replace it was probably a bit of an overkill.  Nevertheless, it does the job and will probably do routing as well without any trouble.  It's an RS 440-442, has a step angle of 1.8 degrees and pulls a maximum of 1 Amp per coil.  It doesn't get as hot as the MY5602 simply because it's much bigger.

Here is the new monster motor:
X right motor

That's more like it!

I performed the same calibration procedure that I did with the Y axis and it moved 80.90 mm after 26000 steps.  That's roughly 3 thousandths of a millimetre per step or 321 steps per millimetre.  Makes the Y axis look a bit poor!  The Z axis should have the same value as the X axis since they use the same mechanism and its motor also has 1.8 degree steps.

A few more odds and ends to tidy up - I soldered the sensor circuitry onto strip board and temporarily taped them onto the X and Y axes.

The sensors:
X and Y sensors

I will devise a better mounting method later.  Right now it's enough to know they work and the drilling platform can work in a purely relative position mode.  Once the sensors are fitted, the drilling platform will be able to know where it is in terms of absolute position.  The Z depth sensor will allow it to work where the tip of the drill bit is but I'm not sure how useful that's really going to be.  You can also just see the wooden plate bolted to the top of the steel plate with a grid pattern glued to the top.

Time to put the finishing touches to it...